Overview...The Bad Attitude
from Hawk
Mountain Enterprises (HM) is a standard kit.
I built the initial configuration as
Hermes 3 (H3) with a
couple of options (75mm MMT in lieu of the
standard 54mm and the larger (3/16") G10 fins).
When I placed my order, I
also ordered a second booster section that is 54"
long that I
used with an HM aluminum fin can in a
minimum-diameter variant for Hermes 4 (H4).

Construction:
The booster section did not require much work
other than finishing and bolting on the fin can.
Since the tube is rather long, I decided to
take it to an auto-body paint shop for painting.
The tube itself was in great shape with only a
few pin-holes that required filling - I used
some of the Bondo surface filling I mentioned in
the Hermes 3 article.
After a wet sanding with 320 grit, I applied
an initial primer coat with RustOleum Plastic
Primer and filled in the few holes. A little
touch-up with primer and another sanding, and
the tube was ready for the paint shop. They
applied two coats of white and a coat of acrylic
gloss clear to protect the water-based paint.
I brought the tube back and applied some
decals and pinstripes in a theme similar to that
of Hermes 3, since the sustainer from that
rocket will be coupled with the new booster.
Back to the paint for a final clear coat (should
have used two coats since some of the pinstripe
pealed away during the initial flight).
Once painted, I cemented a Giant Leap
Slimline 98mm motor retainer to the rear of the
tube - having masked off the rear 3/4" of the
tube prior to painting. The retainer comes with
a flange that is normally supposed to sit in
front of the rear MMT centering ring, but since
this is a minimum-diameter application, I had
the flange parted off in a machine shop to
provide a more aerodynamic profile. I could have
sanded it off on the bench sander, but I wanted
a very clean result and was not sure I could
achieve that on the sander.
I then assembled the fin can around the rear
of the tube, just forward of the motor retainer.
It is a relatively straight forward process and
the included instructions from HM are clear.
I added a couple of rail buttons to the body
tube with Loctite E120-HP super-strength epoxy
and a couple of sheet metal screws that I ground
down to make sure they did not protrude into the
motor cavity - that only allowed about a
half-turn of the screw into the airframe tube,
but with the addition of a bit of the epoxy, it
should help a little with the shear strength of
the button mounting.
I used aluminum buttons since they looked
nice, but I later learned they are really a
no-no out on the range since they gall the rail.
Uh-oh! I guess I will just have to apologize
since the E120-HP works so well! I also had
sanded the bottom of the buttons against a piece
of sandpaper wrapped around a 4" airframe in
order to make them more conforming to the
booster surface.
A 1/4" vent hole for the recovery cavity and
a couple 1/8" holes for the shear pins and the
booster was set to fly! Since this is a
minimum-diameter application, an eyebolt screwed
into the motor's threaded forward-closure will
provide the recovery anchor. A
Fireball provides zipper control in the event
of an early/late drogue deployment.

Everything else forward of the booster is the same as with
Hermes 3.
Flight and Recovery:
The initial flight attempt utilized a AT
M750W slow-burn motor. The loaded weight of
Hermes 4 with this motor is around 35 pounds, so the M750
provides a 6+:1 thrust-to-weight ratio, which
got it off the rail just fine. If the wind is
up, then a better motor choice most likely moves to
an AT M1939W which increases the T-W ratio
something over 11:1.
I flew Hermes 4 on July 11, 2009 -
the plan was to do a test flight on a small
K805, but I found that my Aero Pack 98-75mm motor
adapter would not fit into the rear of the
Slimline motor mount...so, after checking with a
couple of people and having them look over the
construction on the new booster, I decided to go
ahead and roll the dice and go with the big
motor for first-flight.
After building up the Aerotech M750W moonburner motor
(interesting construction requiring epoxying the
grains together to keep the offset bores
aligned),
I
hauled the rocket out to the pad. Launch was very
straight and it roared and coasted to an
altitude of ~21K' (average of the three
recording altimeter readings).

The BeeLine GPS worked perfectly and I recovered
the rocket downwind about 1.8 miles away - the
rocket was in perfect shape except for some of
the pinstriping that apparently didn't like the
sustained time above mach, and one pyro battery
that dislodged on landing (it hit a little
harder than H3 - I used a Sky Angle 60" Classic
II instead of
the 10' Rocketman chute I used on the heavier H3).

Summary:
Very pleased with the overall performance and
quality of the Hawk Mountain components and how
much fun it has been to get to this point - now
on to bigger and better things!!